摘要
胡状集油田是严重的非均质油藏,含水高,油层埋藏深且矿化度高,单一的调剖效果越来越差.为了克服这些难题,提出了双向调堵技术,通过室内实验优选出一种新的交联聚合物体系,评价不同调堵形式的开发效果,验证了双向调堵具有相对的优越性,较之单一的调剖或者堵水,可提高3%采出程度.将该技术应用于现场试验,并取得了显著的增油效果.
Huzhuangji oilfield is a highly heterogeneous reservoir,with high water cut,deep reservoir burial and high salinity,single profile control is getting poorer results.In order to overcome these problems,a bi-way profile-adjusting and plugging technology is proposed,a new crosslinking polymer system is developed through the indoor experiments.Through evaluation of different profiling-plugging methods,the bi-way profiling-plugging is relatively advantageous,recovery degree can be improved by 3%when compared with single profile control or water plugging.Its field application has obtained remarkable effects in oil recovery increase.
作者
赵泽宗
ZHAO Zezong(Pudong Oil Plant.Sinopec Zhongyuan Oilfield Company,Puyang,Henan 457001,China)
出处
《钻采工艺》
CAS
北大核心
2019年第5期45-48,共4页
Drilling & Production Technology
基金
中原油田科技项目“强水淹油藏堵调驱一体化技术研究与应用”子课题“油水井双向调堵工艺技术研究与应用”(编号:2019036)
关键词
胡状集油田
高含水
双向调堵
交联聚合物
Huzhuangji oilfield
high water cut
bi-way profile control and water plugging
crosslinked polymer