期刊文献+

单立管排水系统通水能力的试验研究 被引量:7

Study on flux capacity of single stack drainage system
下载PDF
导出
摘要 研究单立管排水系统的通水能力和气压波动情况,考察底部排出横管管径和排出横管连接弯头等因素对立管压力波动的影响。结果表明,当公称外径dn110的排水立管底部采用2个45°弯头连接dn110的排出横管时,单立管伸顶通气系统的通水能力约为4.8L/s;放大底部排出横管管径并不能有效提高单立管系统的通水能力;设置2个45°弯头连接排出横管稍微改善了立管底部排出的水力条件;本试验测出单立管不伸顶通气系统的通水能力约为3.2L/s。 Water passing capacity and air pressure fluctuation inside the single stack sewer were studied. The influencing factors on air pressure fluctuation in stack, such as the size and the connection bend of outlet horizontal pipe etc were investigated. The results showed that for vertical sewer pipe of nominal diameter of 110 mm with roof ventilation at the top and connected to outlet horizontal pipe of same diameter at the bottom by two 45-degree bends, the flux capacity will be about 4. 8 L/s. To enlarge the size of the horizontal pipe did not enhance the water passing capacity effectively. However, the setup of two bends improved slightly the hydraulic conditions in the bottom of discharge stack. According to this test, the water passing capacity of the single stack system without top ventilation was about 3.2 L/s.
出处 《给水排水》 CSCD 北大核心 2007年第6期65-67,共3页 Water & Wastewater Engineering
关键词 单立管排水系统通水能力的试验研究 Single stack drainage system Water passing capacity Fluctuation of air pressure Outlet horizontal pipe
  • 相关文献

参考文献2

二级参考文献5

  • 1冯旭东.建筑排水立管中外水力计算的比较.见:全国建筑给水排水委员会排水分会第二届第一次学术交流会论文集.宁波,2005.6~13
  • 2刘新超 张玉先 张淼.高层建筑UPVC排水立管通水能力研究[J].给水排水,1997,(6):63-63.
  • 3张晓燕.建筑排水管道内的气压情况试验报告.见:全国建筑给水排水委员会排水分会第二届第一次学术交流会论文集.宁波,2005.59~71
  • 4钟祥璋.PVC低噪声排水管的噪声特性[J].噪声与振动控制,1997,17(3):43-44. 被引量:8
  • 5王文海,吴俊奇,欧云锋.用动态体积法测定卫生洁具排水流量曲线[J].给水排水,2002,28(5):59-62. 被引量:3

共引文献13

同被引文献34

引证文献7

二级引证文献29

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部