摘要
通过对澄碧河水库大坝混凝土心墙防渗效果和土坝变形观测资料分析认为:大坝混凝土心墙防渗作用显著,但坝体填土质量差是造成坝顶心墙两侧路面不均匀沉陷的主要原因,观测资料表明,大坝沉陷、水平位移符合土坝变形规律,大坝抗滑稳定安全。
By analysis on seepage prevention effect of the concrete core wall and deformation monitoring data of the earth filleddam, conclusion was gotten that the concrete core wall was effective in seepage prevention, and low earth filling quality was the main reason for uneven settlement of the crest of clay core wall.Monitoring data showed that dam settlement and horizontal displacement was of regularity, and the stability against sliding was high.
出处
《大坝与安全》
2009年第3期15-19,22,共6页
Dam & Safety
关键词
澄碧河水库
混凝土心墙
粘土心墙
不均匀沉陷
原型观测资料
Chengbihe reservoir
concrete core wall
clay core wall
uneven settlement
prototype observation data