期刊文献+

澄碧河水库土坝坝顶不均匀沉陷与安全运行分析 被引量:1

Analysis on uneven settlement of crest and safety operation of Chengbihe dam
下载PDF
导出
摘要 通过对澄碧河水库大坝混凝土心墙防渗效果和土坝变形观测资料分析认为:大坝混凝土心墙防渗作用显著,但坝体填土质量差是造成坝顶心墙两侧路面不均匀沉陷的主要原因,观测资料表明,大坝沉陷、水平位移符合土坝变形规律,大坝抗滑稳定安全。 By analysis on seepage prevention effect of the concrete core wall and deformation monitoring data of the earth filleddam, conclusion was gotten that the concrete core wall was effective in seepage prevention, and low earth filling quality was the main reason for uneven settlement of the crest of clay core wall.Monitoring data showed that dam settlement and horizontal displacement was of regularity, and the stability against sliding was high.
出处 《大坝与安全》 2009年第3期15-19,22,共6页 Dam & Safety
关键词 澄碧河水库 混凝土心墙 粘土心墙 不均匀沉陷 原型观测资料 Chengbihe reservoir concrete core wall clay core wall uneven settlement prototype observation data
  • 相关文献

同被引文献8

引证文献1

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部