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旋转进气畸变对轴流压气机气动稳定性影响实验研究 被引量:12

Effects of Rotating Inlet Distortion on a 5-Stage HP-Compressor Stability
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摘要 利用RB-1995级高压压气机,实验研究了进口旋转总压畸变对其性能和气动稳定性的影响,获得了总压畸变的旋转频率对高压压气机喘振裕度损失的影响结果。结果表明:正转时,减少了压气机的喘振裕度,并且存在2个危险频率,出现损失峰值;反转时,对喘振裕度影响较小,甚至提高了压气机的喘振裕度。 The inlet flow rotating distortion effects in a five-stage HP compressor have been investigated experimentally。For co-rotating distortions,the results exhibited significant loss in stability margin and there were two peaks in surge margin degradation corresponding to two distortion rotating frequencies;For counter rotational distortions,the tests showed minimal loss of stability margin,especially in some cases.The range of stable operations was even enlarged.
作者 李传鹏 胡骏
出处 《航空动力学报》 EI CAS CSCD 北大核心 2004年第4期433-437,共5页 Journal of Aerospace Power
关键词 航空、航天推进系统 压气机 旋转畸变 喘振裕度损失 aerospace propulsion system compressor rotating distortions surge margin degradation
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  • 3Longley J P,Shin H W,Plumley R E,et al. Effects of Rotating Inlet Distortion on Multistage Compressor Stability[J].ASME Journal of Turbomachinery, 1996,118:181 - 188.
  • 4peters T,Fottner L. A Coupled Steady-Unsteady State Data Acquisition System for the Investigation of Rotating Inlet Distortion at a Multistage Compressor Test Facility [R].Firenze , Ilaty : Proceedings of the 15th Bi-Annual Symposium on Measuring Techniqu

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