摘要
本文从濮 65气藏的概况出发 ,对该气藏的开发历程进行了分析 ,利用新井的 RFT资料、老井测压和试井、动态分析资料 ,对该气藏的天然气的储量动用状况和潜力进行分析 ,部署了产能恢复方案 ,通过分年度逐步实施 ,获得了很好的开发效果和比预期好的开发效益 ,为老气藏产能恢复 ,提高开发水平和开发效益提供了有益的借鉴。
This thesis is from the general situation of the Pu 65 gas reservoir and the process of development of the gas reservoir is analysed. Using the data of new well RFT and the data of old well that pressure measurement, well testing and dynamic analysis , the gas reserves draw up on and potentiality of the gas reservoir is analysed.The productivity instauration project is deployed. The good development result and the all the better benefit of development compare to expectation acquired by being carried out gradually with year after year.It provide the beneficial experience for old gas reservoir in productivity instauration, exaltation development level and benefit of development.
出处
《内蒙古石油化工》
CAS
2005年第1期69-71,共3页
Inner Mongolia Petrochemical Industry
关键词
濮65气藏
生产能力
经济效益
评价方案
凝析气藏
储层
孔隙度
condensate gas reservoir
process of development
reserves draw up on productivity instauration
benefit of development