摘要
四米龙门刨床错位无环流可逆调速系统进行系统调试时,遇到一系列抗干扰的问题.本文仅研究、分析触发脉冲干扰和电动机爬行问题,分析产生的原因,提出解决办法,使系统可靠地工作.
In systematic adjustment of the convertible and speed-adjustable system with dislocation and unloop current for 4 meters range planner, some anti-interference problems were met. In this paper, interference of trigger pulse, motor creep and their resulting causes are studied and analyzed. The solving method for the reliable operation of the system is presented.