摘要
卫95块原始储层的层间、平面矛盾导致了注水开发中后期二、三类储层动用状况差,平面波及体积小,调剖、酸化等改善吸水剖面的措施效果逐年变差,目前吸水厚度仅占射孔厚度的41.7%,层间矛盾加剧。通过有针对性地提出调剖、解堵转向注水工艺,实现了层间、层内、平面的注水方向、强度转向.实施调剖了39井次,酸化24井次的效果为:吸水厚度增加12%,水驱控制程度提高7%,水驱动用程度提高7.5%,平均注水压力下降1.5MPa,日注水能力上升。见效增油8 500 t,自然递减减缓1%,采收率提高1%。
Those contradictions among layer and level cause two serious phenomenon appeared.The use of two-and-three-rate reservoir bed became bad middle and later periods of water flooding development,involved the volume diminished,and the effect of adjust and drive and solve and stop up became bad year by year.Thickness that absorbed water only occupy thickness of perforation 41.7%,contradictions among layer were aggravate at present.So the craft of adjust and drive,solve and stop up,change direction of water flooding directly were presented.It can change direction of water flooding among layer and level.After adjust and cut open 39 wells and acid 24 wells,thickness that absorbed water increased 12%,the degree of water drove controlling improved 7%,the degree of water drives using improved 7.5%,the average pressure of water flooding declined 1.5MPa,the ability of water flooding increased every day.Then the oil increased 8500t,natural decrease slew down 1%,and the petroleum extraction received rate raised 1%.
出处
《西南石油学院学报》
CSCD
北大核心
2005年第5期57-61,共5页
Journal of Southwest Petroleum Institute
关键词
调剖
解堵
转向注水
adjust and drive
solve and stop up
change direction of water flooding