摘要
某电厂捷制机组在采用以机跟炉随为基础的协调控制(CTF)方式后,实现了机组自动发电控制(AGC)。在协调控制系统投入的实践中,通过修改控制策略解决了负荷控制响应和压力控制的波动问题。现场运行表明,所做的控制系统完善工作是有效的,协调控制系统效果比较理想。
A czechic 200MW dynamoelectric unit successfully put in Coordinated Control Turbine Follow Mode, carried out AGC This paper introduces the load control response and pressure control fluctuation problems solved through correcting strategy. On-site experiments indicate that all the improvement work on CCS is effective and the control effect of CCS is ideal.
出处
《电力学报》
2005年第4期372-374,共3页
Journal of Electric Power
关键词
协调控制
DCS
单元机组
cooreinate control
DCS
generating unit.