期刊文献+

连续刚构桥底板崩裂事故的评析 被引量:57

Analysis of Accident of Bursting Crack in Bottom Slab of a Continuous Rigid-Frame Bridge
下载PDF
导出
摘要 针对某连续刚构桥在施工过程中发生的底板崩裂事故,通过全面的计算,分析事故原因,确认在张拉跨中合龙束时底板崩裂是由合龙束产生的径向下崩力所致;并对该桥型类似问题进行剖析,给相关设计提供参考和建议。 For the accident of bursting crack occurring in bottom slab of a continuous rigidframe bridge at construction stage, this paper analyzes the causes leading to the accident through all-round and thorough calculation, and confirms that the bursting crack was caused by radial downward bursting force coming from closure prestressing strands at the time the strands at midspan were tensioned. Meanwhile, the paper also analyzes problems of the type of the bridge similar to the accident mentioned above with an aim to providing references and suggestions to the design related to.
出处 《世界桥梁》 北大核心 2006年第1期66-69,共4页 World Bridges
关键词 连续刚构桥 崩裂 径向力 等效荷载法 事故分析 continuous rigid-frame bridge bursting crack radial force equivalent load method accident analysis
  • 相关文献

参考文献4

二级参考文献3

  • 1陈玮.[D].重庆交通学院,2004.
  • 2周志祥.高等钢筋砼结构[M].北京:人民交通出版社,2002..
  • 3卢树圣.现代预应力砼理论与应用[M].北京:中国铁道出版社,2000..

共引文献58

同被引文献178

引证文献57

二级引证文献206

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部