摘要
大冶特钢以传统工艺EAF+LF-轧制250mm×250mm轧坯生产的30CrMnSiA合金钢1.2t电渣锭母材,钢锭上部易产生裂纹。经采用优化工艺EAF+LF(VD)-Φ320mm铸棒生产ESR母材,并控制母材中(%):≤0.003Pb、≤O.015Sn、≤0.030As、≤O.015(Pb+Sn)及0.020~0.035Ti;供电与水温均用计算机控制。结果使ESR充填比由0.40提高至0.53,电渣电耗下降200kWh/t,母材至电渣锭的金属收得率由82.41%提高至93.75%,废品量由109.55kg/t降低到29.42kg/t,生产周期缩短7~10天。
Traditional process to produce electrode of alloy steel 30CrMnSiA 1.2 t ESR ingot at Daye Special Steel is EAF + LF - rolling 250 mm x250 mm Billet, by which the crack easily produced at top of ESR ingot. With using optimum process to produced ESR electrode: EAF + LF(VD) steelmakiug - Φ320 mm cast round electrode, controling ≤0. 003Pb, ≤0. 015Sn, ≤0. 030As, ≤0. 015( Pb + Sn) and 0. 020 ~ 0. 035Ti in electrode, power supplying and water temperature controlling by computer, the ESR filling ratio increased from 0. 40 to 0. 53, ESR electrical power consumption decreased by 200 kWh/t, metal yield of ESR ingot/electrode increased from 82. 41% to 93.75%, rejected metal decreased from 109. 55 kg/t to 29. 42 kg/t and production period shortened by 7 ~ 10 days.
出处
《特殊钢》
北大核心
2007年第1期49-50,共2页
Special Steel
关键词
电渣钢锭
表面质量
工艺优化
ESR Steel Ingot, Surface Quality, Process Optimization