摘要
景区污水排放量增加且进水NH3-N含量过高,导致出水NH3-N严重超标。改造工程在充分利用原有构筑物的基础上,增加了曝气硝化池、污泥浓缩池和污泥回流系统,改造后出水水质达到《污水综合排放标准》(GB 8978—1996)新改扩一级标准。
The effluent NH3 - N could not meet the discharge standard, because of the discharge quantity increase and high content of NH3 - N in the influent. Based on the former treatment system, aerated nitrification tank, sludge thickening tank, sludge return system were added in reconstruction project. After the reconstruction, the effluent quality meets the first class criteria of Integrated Wastewater Discharge Standard ( GB 8978 - 1996).
出处
《中国给水排水》
CAS
CSCD
北大核心
2007年第22期27-29,共3页
China Water & Wastewater
基金
广西科学基金资助项目(桂科基0575103)
广西科学基金资助项目(桂科自0679010)
关键词
景区污水
曝气硝化
生物接触氧化
污泥回流
sewage in scenical site
aerated nitrification
biological contact oxidation
sludge return