期刊文献+

大庆油田萨南东部过渡带注CO_2驱油先导性矿场试验研究 被引量:54

A pilot test and research on oil displacement by injecting CO 2 in eastern Sanan of Daqing oilfield.
下载PDF
导出
摘要 1988年大庆油田在萨南东部过渡带开辟了注CO2试验区,1990年至1995年底先后对葡Ⅰ2油层和萨Ⅱ10~14油层进行了非混相CO2驱油先导性矿场试验。两次试验均采用先进行前期水驱,尔后进行水、气交替注入方式,CO2气体注入总量各为0.2PV左右。矿场试验用的CO2是大庆炼油厂的副产品,纯度为96%。这两次矿场试验结果表明,降低了水油比和水驱剩余油饱和度,采收率提高6.0%OOIP,每增采1t原油需注入2200m3CO2气体。 In 1988, a pilot area for CO 2 injection was selected in the transitional zone of the eastern Sanan of Daqing oilfield. From 1990 to the end of 1995, two pilot tests of non miscible CO 2 flooding were conducted in the Payzone Pu Ⅰ 2 and Payzone Sa Ⅱ 10~14 successfully. In both the tests, water flooding was performed and then water alternating with gas process. The gross quantity of CO 2 injected in both tests was 0.2PV or so respectively. The CO 2 used in the tests is a by product from Daqing oil refining plant, its purity is 96%. The results of both the tests show that both water oil ratio and residual oil saturation have dropped and the recovery efficiency has increased by 6.0% OOIP. 2200m 3 of CO 2 will be needed to 1 ton oil produced.
出处 《油气采收率技术》 CSCD 1997年第3期13-19,41,共8页
关键词 二氧化碳驱油 驱替试验 油田 tertiary oil recovery, CO 2, injecting alternatively, displacement test, performance, result, recovery efficiency,Daqing oilfield
  • 相关文献

同被引文献490

引证文献54

二级引证文献725

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部