期刊文献+

跨音风扇激波/漏流涡干扰模型探讨 被引量:1

A MODEL OF INTERACTION BETWEEN SHOCK WAVE AND LEAKAGE VORTEX ON TRANSONIC FAN
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摘要 激波/漏流涡干扰系旋转运动与突然的逆压力梯度的强相互作用,引起各自形态和强度发生变化。涡破裂对风扇/压气机效率和稳定性十分不利。本文探讨了激波/漏流涡干扰的物理模型,通过求解涡核运动方程,分析了涡核特征参数对涡破裂的影响,为控制涡破裂提供了根据。 A strong interaction between shock wave and leakage vortex,induced by an intensive inter-impact of rotating motion on abrupt anti-pressure gradient,makes their formations and strengths varied.The vortex breakdown deteriorates the stability and efficiency of compressor and fan.So a model of interaction between shock wave and leakage vortex is formulated.The solution of vortex core movement equations shows that the small initiative vortex core velocity and enhanced initiative vortex core pressure will induce the vortex instability.The high Mach number and circulation gradient outside the vortex core will result in breakdown of the vortex.The analysis of the factors leading to vortex breakdown serves as a foundation for its controlling.
出处 《航空动力学报》 EI CAS CSCD 北大核心 1998年第3期225-229,共5页 Journal of Aerospace Power
关键词 跨音速 压气机 激波 干扰 漏流 涡轮风扇发动机 Transonic compressor Shock wave Interaction Numerical calculation
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参考文献4

  • 1杨智,硕士学位论文,1995年
  • 2Kang S,ASME 92-GT-432,1992年
  • 3Chen G T,ASME 90-GT-153,1990年
  • 4林炳秋,空气动力学学报,1988年,6卷,1期

同被引文献9

  • 1袁巍,周盛,陆亚钧.压气机间隙流与处理机匣作用的三维数值分析[J].北京航空航天大学学报,2004,30(9):885-888. 被引量:27
  • 2Ingo Wilke,Hans-Peter Kau. A numerical investigation of the flow mechanisms in a high pressure compressor front stage with axial slots[J]. ASME Journal of Turbomachinery, 2004,126 ( 3 ) : 339-349.
  • 3Behnam H B, Joao A T, Paul C, et al. Parametric study of tip clearance casing treatment on performance and stability of a transonic axial compressor[J]. ASME,2004,126(4):527-535.
  • 4Wilke I,Kau H P. A numerical investigation of the influence of casing treatments on the tip leakage flowin a HPC front stage[R]. GT 2002-30642,Amsterdam,The Netherlands:ASME, 2002.
  • 5Louise F M, Lyle D D, Paul D O, A CFD study of the flow through a transonic compressor rotor with large tip clearance[R]. AIAA Paper 2004-3934,Fortlauderdale Florida: [s. n. ],2004.
  • 6Holfman W, Ballmann J. Tip clearance vortex development and shock-vortex-interaction in a transonic axial compressor rotor [R]. AIAA 2002-0083,Reston,V A:[s. n. ],2002.
  • 7朱俊强,刘志伟.4 种不同型式机匣处理的实验研究及机理分析[J].航空学报,1997,18(5):567-570. 被引量:13
  • 8李玲,于清,陆亚钧.处理机匣在单级跨声速风扇上的实验研究[J].推进技术,2000,21(3):49-52. 被引量:8
  • 9程荣辉.轴流压气机设计技术的发展[J].燃气涡轮试验与研究,2004,17(2):1-8. 被引量:51

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