摘要
为了分析同心扬水三泵站出水渡槽在加固维修后,出现水流紊乱的原因,采用迭代法计算渡槽正常水深和临界水深,并且实现了自动计算和自动判断水面线形状以及推求水面线的程序.通过对渡槽内水面线进行计算并与实测水深比较,得出两者误差较小、吻合较好.根据计算和分析结果表明,加固维修第17节和23节槽壳后,使得槽内水流紊乱,并且部分槽壳行水断面不够.因此,建议更换第17节和23节槽壳,以使渡槽中的水流平顺通过,满足下游灌溉需水流量的要求.
The study was to seek iterative formula of normal water depth and critical water depth of the outlet aqueducts in the NO.3 pump-station. Main reasons of the turbulence flow in the aqueducts are analyzed. Normal water depth and critical water depth of the aqueducts are computed by using iteration method. The types of water surface profiles are confirmed. So, water surface profiles of the outlet aqueducts are computed using partition summation method. Through comparing calculation results with experiment datas, it shows that its fit well. The procedure is short-cut and correct. In order to flow smoothing and satisfy downstream irrigation, proposed to replace section 17 and 23 shells of the aqueducts.
出处
《宁夏工程技术》
CAS
2009年第3期275-277,281,共4页
Ningxia Engineering Technology
基金
国家自然科学基金资助项目(10671157)
宁夏高校自然科学基金项目(2007JY010)
国家民委科研项目(09BF07)
关键词
渡槽
水力计算
迭代法
水面线
aqueduct
hudraulic computation
water surface profiles