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Reasons resulting in the collapsed tubing near wellhead in high pressure and high temperature deep well during well testing and measures to prevent the collapsing

Reasons resulting in the collapsed tubing near wellhead in high pressure and high temperature deep well during well testing and measures to prevent the collapsing
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摘要 Because various reasons, the tubing near wellhead was collapsed during well testing in high pressure and high temperature deep well when the outer pressure was less than collapsing strength. To find the reasons in the abnormally collapse and countermeasures, first the quality of the tubing was checked. It was founded that the collapse was not resulted from the defect of the tubing. Then, force and stress exerted in the tubing was analyzed taking XS2 well as an example. The analysis results were concluded as follows. The collapsing strength of tubing decreased due to the axial tensile, which is seriously at the upper tubing especially. During injecting, the additional axial force that was caused by the temperature effect increased the tubing near wellhead to suffer axial tensile and further reduced the collapsing strength of tubing near wellhead. Reinforcing defect, prohibiting defect tubing to trip in hole, according to the calculation to impose appropriate annular pressure, selecting size nozzle to reverse pumping and controlling the reverse pumping speed and pressure, prohibiting to be opened flow and reducing or releasing the annular pressure can prevent the well testing tubing down-hole being collapsed at the wellhead.
出处 《Journal of Energy and Power Engineering》 2009年第9期41-44,66,共5页 能源与动力工程(美国大卫英文)
关键词 high pressure and high temperature deep well well testing: tubing COLLAPSE analysis 油管 井口 原因 高温 高压 外部压力 试井 塌陷
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