摘要
针对国华电力公司17台600 MW亚临界锅炉再热汽温普遍低于设计值的现象,从受热面设计、运行调整以及协调控制等方面分析了再热汽温偏低的原因,提出了综合治理再热汽温低的思路和方法。
Aiming at the problems that the actual reheat steam temperature of the 17 boilers for 600 MW subcritical power units in Guohua Electric Power Co.,Ltd.were lower than their design values,a cause analysis was performed from aspects of heat surface design,operation adjustment and coordination control etc.,after which corresponding countermeasures are proposed.
出处
《发电设备》
2010年第3期199-201,共3页
Power Equipment
关键词
锅炉
再热汽温
受热面
boiler
reheat steam temperature
heat surface