摘要
通过降低轧制速度,增加粗轧道次压下量特别是后几道次的压下量,使GCr15轴承钢150 mm×150mm铸坯连轧成Φ30~45 mm材的低倍质量明显提高,缩孔出现率由改善轧制工艺前的26%~46%降至0,超声波探伤合格率100%,一般疏松级别0~1,中心疏松级别1~1.5。
With decreasing rolling speed, increasing reduction in rough rolling passes especially in last passes, the quality of macrostructure of continuous roiling Ф30 -45 mm round products of bearing steel GCr15 roiled from 150 mm × 150 mm casting billet increases obviously i.e. occurred ratio of residual shrinkage hole decreases to 0 from 26% - 46% before improvement of rolling process, qualified ratio of ultrasonic detection is 100% , rating of general porosity is 0 - 1 and rating of center porosity is 1 - 1.5.
出处
《特殊钢》
北大核心
2010年第5期42-44,共3页
Special Steel
关键词
GCR15轴承钢
棒材连轧
缩孔残余
道次压下量
工艺改善
Bearing Steel GCr15, Continuous Rolling for Bar Products, Residual Shrinkage Hole, Reduction in Pass, Process Improvement