摘要
樊151块为低渗透滩坝砂油藏,储层整体物性差,注水过程中水井注入压力越来越高。针对这一问题,室内评价了储层的敏感性、润湿性、水质配伍性,系统分析了注水井吸水能力变差的原因,然后优化了转注工艺及注水体系,并进行了现场试验,效果良好,实现了樊151块稳定注水,从而提高了储量动用率及最终采收率。
Block Fan 151 is a beach-bar sand reservoir with low permeability.The overall physical property of reservoir is poor.The injection pressure becomes higher and higher during the process of water injection.Aiming at this problem,the sensibility,wettability and water compatibility of reservoir were evaluated in laboratory.The reason of poor water absorbing capacity of injection well was analyzed systematically in this paper.The converted process and water injection system were optimized and the field test was done with a good result.The stable water injection of Block Fan 151 was achieved and the producing rate of reserves and ultimate recovery were improved.
出处
《断块油气田》
CAS
北大核心
2010年第5期596-598,共3页
Fault-Block Oil & Gas Field
基金
中国石化科技攻关项目"博兴洼陷沙四段薄互层低渗透油藏开发配套技术研究"(P05024)部分成果
关键词
低渗透油藏
注水
敏感性
注水优化设计
low permeability reservoir
water injection
sensibility
optimal design of water injection.