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卡马水库大坝滑塌原因分析

Causes for dam slump of Kama Reservoir
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摘要 在抢险记录、事后现场调查、补充地质勘察、现场检测与监测等基础上,对卡马水库大坝的滑塌原因进行分析。通过对导流洞水击振动荷载的估算以及坝坡稳定分析,认为卡马水库大坝坝坡偏陡、稳定安全系数偏小是导致坝体滑塌的内因;导流洞水击振动荷载作用是造成坝体滑塌的外因。建议在大坝加固措施实施前,应保证水库安全泄洪,维持水库低水位运行,确保大坝安全;在加固措施实施时做好施工组织计划及应急预案。 Based on the emergency records,field investigations,additional geological surveys,field inspections and monitoring and design and construction information,the causes for the dam slump of Kama Reservoir were analyzed.By estimating the vibration loads of water hammer of the diversion tunnel and analyzing the dam slope stability of Kama Reservoir,the steep slope of Kama Reservoir dam and its insufficient stability safety were regarded to be the internal causes for the dam slump,and the vibration load of water hammer of the diversion tunnel was the external causes.It was suggested that the safety of flood discharge of Kama Reservoir should be guaranteed and the low operating water level should be maintained so as to too ensure dam safety before implementing rehabilitation programs.
出处 《水利水电科技进展》 CSCD 北大核心 2010年第6期63-66,共4页 Advances in Science and Technology of Water Resources
基金 "十一五"国家科技支撑计划(2006BAC14B05 2006BAC14B07) 南京水利科学研究院基金(Y710002)
关键词 卡马水库 大坝滑塌 水击 振动荷载 坝坡稳定计算 Kama Reservoir dam slump water hammer vibration load stability calculation of dam slope
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  • 1李雷,龙智飞,张士辰,等.广西壮族自治区罗城仫佬族自治县卡马水库大坝安全评估及处置对策研究[R].南京:南京水利科学研究院;河池:广西河池水利电力勘测设计研究院,2009.

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