摘要
为解决生产窄口,提高生产效率,减少能源消耗,降低生产成本,将某产品用黄铜壳体压底工序进行工艺改进,通过优化模具设计,合理分配各部分金属变形,保证金属流线的连续性,更换加工设备,实现了该黄铜壳体压底工序由4次改为2次。
To solve the key problem in production, improve the production efficiency, reduce energy consumption, lower production cost, the pressing bottom process was improved for the brass shell of a product. Through optimizing mold design, reasonable distribution of the metal, pattern of deformation to ensure continuous metal flow, replacing the processing equipment, the times of pressing bottom process for the brass shell was changed from four to two.
出处
《精密成形工程》
2011年第5期59-62,共4页
Journal of Netshape Forming Engineering
关键词
压底
工艺改进
金属流线
黄铜壳体
pressing bottom
process improvement
metal flow line
brass shell