摘要
白莲崖水库大坝初次蓄水后,部分坝基渗透压力较大、局部扬压力系数高于设计值,从地质、设计、施工、运行等多方面进行了分析,并提出了处理意见。
After first impoundment of Bailianya reservoir, high seepage pressure and uplift pressure exceeding designed value occurred at some dam blocks. This paper analysed the cause reasons in aspects such as geology, design, construction and operation. Further, treatment advices were presented.
出处
《大坝与安全》
2011年第4期28-30,共3页
Dam & Safety
关键词
坝基
渗压
原因
分析
dam foundation
seepage pressure
cause reason
analysis