摘要
在测量船某型号任务的数据处理过程中,通过比对两套外测设备的原始测量数据,发现方位角的系统误差偏大。针对设备严重超出精度指标的问题,通过进一步的试算,利用箭载GPS数据进行比对,仔细分析了引起方位角系统误差偏大的各种因素,逐步排查后找出了问题原因,并由船载设备进行修正。通过排查分析,验证了船载设备零值修正处理方法的正确性,为船载系统类似问题的解决积累了经验。
In data processing of a task by space TT&C ship, it is found out that the azimuth error is relatively large through comparing the data of two measurement equipment. By calculating and comparing the data of rocket - borne GPS, possible factors causing the large azimuth error are analysed and the reason is found. The error is corrected by equipment onboard ship. The zero - value correction method proposed is validated through investigation and analysis, which provides reference for such problems.
出处
《电讯技术》
北大核心
2011年第10期71-75,共5页
Telecommunication Engineering
关键词
航天测量船
数据处理
系统误差
方位角测量
零值修正
space TY&C ship
data processing
system error
azimuth measurement
zero- value correction