摘要
针对风镐缸体铸件存在的缺陷,分析了原铸造工艺及产生缺陷的原因,找出ADI风镐缸体铸件铸造过程中的难点,提出了改进工艺方案,并通过加强熔炼及热处理的操作规范性,减少了铸件缺陷的产生,提高了产品的质量和合格率,降低了生产成本。
Aiming at the defects existing in the pneumatic cylinder castings,the original casting process and the causes of defects were analyzed,the difficulty of ADI(Austempered Ductile Iron) cylinder in casting process was found,the improvement scheme was put forward.Using improved process,combining strengthening smelting and heat treatment operation standard,the casting defects reduce,the product quality and the qualified rate improve,the production cost reduces.
出处
《铸造技术》
CAS
北大核心
2012年第4期467-468,共2页
Foundry Technology
基金
江苏省高校科研成果产业化项目(项目编号:JH08-48)
常州市中小企业基金项目(项目编号:CE2008008)
关键词
风镐缸体
ADI
铸造工艺
工艺改进
pneumatic cylinder
ADI
casting process
process improvement