摘要
2009年9月11日莲花四号机水导发电油面上涨约60mm,为水导冷却器漏水所致。在缺陷处理中,不破坏水导瓦间隙值,不用尾水蜗壳排水,采用在机坑内中心定位的方法,改进了工艺,提前了工期,提高了工效。同时,对冷却器铜管泄漏原因进行了分析。
On September 1 lth 2009, it was found that leakage of oil cooler of turbine guide bearing at unit No. 4 of Lian- hua hydropower station occurred. During treatment, to protect the clearance of turbine guide bearing segments and not to discharge by tailrace spiral case, central positioning in the turbine pit was adopted. In this way, technique improvement and higher efficiency were achieved. Further, the cause reasons of leakage were analyzed.
出处
《大坝与安全》
2012年第2期54-55,共2页
Dam & Safety
关键词
莲花四号机
水导油混水
油冷却器泄漏
工艺改进
unit No.4
water infiltration into turbine guide bearing oil
leakage of oil cooler
technique improvement