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液化天然气罐用9%Ni钢板坯连铸工艺优化 被引量:2

Optimization of Slab Concasting Process of 9%Ni Steel for Liquefied Natural Gas Tank
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摘要 分析了9%Ni钢(/%:≤0.10C、≤0.35Si、0.30~0.80Mn、≤0.005S、≤0.008P、8.5~10.0Ni、≤0.10Mo、≤0.10Al)200~220 mm板坯连铸试生产中出现的结晶器液面结壳、铸坯表面网裂纹产生原因,对连铸工艺进行优化。结果表明,液相线温度偏差是导致9%Ni钢液面结壳的主要原因,基于差示扫描量热法(DSC)的实测数据建立了新的液相线温度计算公式,得出试验的9%Ni钢的液相线温度,在钢水过热度为10~30℃时能较好地满足板坯的连铸要求。通过控制[N]≤25×10^(-6),[Al]≤0.03%,二冷比水量由0.6L/kg降至0.4L/kg,使9%Ni钢连铸顺行,铸坯内部和表面质量良好。 The formation causes of occurred shell at meniscus in mold and network crack of slab surface in pilot con-casting production of 200 - 220 mm slab of 9% Ni steel (/% : ≤0. 10C, ≤0. 35Si, 0. 30 - 0. 80Mn, ≤0. 005S, ≤ 0. 008P, 8.5 - 10. 0Ni, ≤0. 10Mo, ≤0. 10Al) are analyzed, and the optimization on concasting process has been carried out. Results show that the calculated deviation of liquidus temperature of 9% Ni steel is the main cause led to the shell oc-curred at meniscus, and based on experimental data by differential scanning calorimetry ( DSC), a new liquidus tempera-ture calculation formula is established to get the liquidus temperature of tested 9% Ni steel, and as the overheat extent of liquid is 10 -30 ℃, it is available to meet the requirement of slab concasting. With controlling [ N] ≤ 25 x 10^-6, [ Al] ≤0. 03% and decreasing secondary cooling water rate from 0. 6 L/kg to 0. 4 L/kg the concasting of 9% Ni steel is going on smoothly, the inner and surface quality of slab is nice.
出处 《特殊钢》 北大核心 2012年第5期29-31,共3页 Special Steel
关键词 9%NI钢 板坯 连铸 液面结壳 网状裂纹 工艺优化 9% Ni Steel, Slab, Concasting, Shell at Meniscus, Network Crack, Process Optimization
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