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水平井注CO_2、降黏剂复合热采技术在毛8块的应用 被引量:3

Application of Compound Thermal Recovery Technology for Horizontal Well Injecting CO_2 and Viscosity Breaker in Mao-8 Block of Zhagan Sag
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摘要 针对毛8块中深层、中低渗、低温低压普通稠油的油藏特征,进行了CO2与毛8块原油溶解降黏实验,在此基础上开展了10口水平井的CO2、降黏剂复合热采技术矿场试验,对影响热采效果的因素进行了分析。结果表明,水平段长度、钻遇率、油层物性及注汽质量等是影响热采效果的主要因素。 The Mao-8 block in Zhagan sag is characterized by ordinary heavy oil reservoir of middle-deep strata, medium-low permeability anti low temperature and pressure, based on which the experiments of solubility and viscosity reduction between C02 and Mao-8 block crude oil are conducted. The pilot tests of 10 horizontal wells are conducted using CO2 and viscosity breaker compound thermal recover3 technology, and the factors influencing the thermal recovery effects are analyzed. The results show that horizontal interval length, drilling encounter rate, reservoir physical property and steam injection quality are the main factors.
出处 《新疆石油地质》 CAS CSCD 北大核心 2013年第2期213-214,共2页 Xinjiang Petroleum Geology
关键词 稠油 热采 二氧化碳 蒸汽吞吐 heavy oil thermal recovery CO2 steam stimulation
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