摘要
基于工程实例对软基中某无铰拱桥桥台位移进行有限元分析,讨论分析过程中特殊非线性的处理方法,并在原设计基础上对桥台进行优化分析。研究结果表明:优化后桥台位移减小,且与实测值吻合,结构内力分布更加均匀,结构处于安全状态,从而也证明本文分析的合理性,所提出的优化变更方案是切实可行的,达到了预期的效果,对同类工程问题具有参考价值。
Based on project example, the displacement of a hingless arch bridge abutment which is in soft ground was analyzed by using finite element software. A processing method of special nonlinear problem was discussed in the analysis process, and the original design was optimized. The results show that the displacement of the abut- ment is decreases after optimization, and it is consistent with the measured value. Meanwhile the internal force distribution is more uniform, and the structure is under a safe state. The analysis in this paper is reasonable, and the optimization program is feasible, which has obtained the expected effect. The results have reference value for similar projects.
出处
《铁道科学与工程学报》
CAS
CSCD
北大核心
2013年第3期7-10,共4页
Journal of Railway Science and Engineering
基金
国家自然科学基金资助项目(51178470)
关键词
无铰拱桥
桥台位移
有限元
优化方案
hingless arch bridge
abutment' s displacement
finite element
optimization program