摘要
分析了S355JR和S355J2低碳钢(/%:0.17~0.20C、0.30~0.55Si、1.40~1.60Mn、≤0.020P、≤0.015S、0.020~0.040A1、0.020~0.030Nb)28~40 t钢锭轧成230~400 mm钢板出现的开裂和穿孔缺陷。通过提高浇钢工操作水平,根据钢水过热度控制本体浇铸和帽口浇铸时问;控制精炼终点[O]≤25×10^(-6)以及钢中铝含量0.020%~0.040%等优化浇铸工艺措施使钢锭探伤合格率提高到96.8%。
An analysis on cracking and perforation defects occurred in 230 ~ 400 mm plates rolled from 28 ~ 40 t ingot of low carbon steel S355JR and S355J2 (/% : 0. 17 ~ 0. 20C, 0. 30 ~0. 55Si, 1.40 ~ 1.60Mn, ≤0. 020P, ≤0. 015S, 0. 020 ~0. 040A1, 0. 020~0. 030Nb) is emTied out. With the optimum process measures including increasing level of op- eration crews, controlling ingot body and hot top casting speed according to overheating extent of liquid, controlling refining end [O]≤25 ×10^-6 and aluminium content in steel 0. 020%~0. 040% , the ingot qualified ratio by nondestructive testing increases to 96.8%.
出处
《特殊钢》
北大核心
2013年第4期36-39,共4页
Special Steel
关键词
低碳钢
28~40t大型钢锭
厚板
轧板开裂
穿孔缺陷
工艺优化
Low Carbon Steel
28 ~ 40 t Large-Scale Ingot
Heavy Plate
Cracking of Rolled Plate
PerforationDefect
Process Optimization