摘要
油田采出水中含有大量的硫酸盐还原菌、腐生菌、铁细菌等,其腐蚀性强,引起采出水回注井井筒注水管柱严重腐蚀,在满足现有注水管柱工作参数条件下,通过改变注水管柱材质、结构的方法,设计出一种抗腐蚀性能强的柔性复合油管。进行了油管强度校核、室内性能评价实验、注水管柱组合设计和现场试验研究。试验表明:柔性复合油管在现有注水工作参数条件下,使用寿命可达15 a以上,达到了钢质油管寿命的3倍以上,为油田注水井井筒防腐提供了一种新方法。
there are lots of sulfate reducing bacteria(SRB),saprophytic bacteria and iron bacteria in oil field produced water whichis highly corrosive substances.So the corrosion in produced water injection well is severe.Under the conditions of meeting the existingwater injection well string working parameters,the anti-corrosion flexible composite injection string was developed by changing the materialand structure of water injection well string.The pipe strength check,indoor performance evaluation experimental,injection stringcombination design and field application study were done to test the flexible composite pipe behavior.The results showed that the flexiblecomposite pipe can be used for more than15 years in existing water injection working conditions,which is more than three times of steeltubing life.Successfully application means a breakthrough and supplies a new method for corrosion resistance of injection well string.
出处
《石油钻采工艺》
CAS
CSCD
北大核心
2013年第4期111-113,共3页
Oil Drilling & Production Technology
基金
中国石油低碳关键技术研究"低渗透油气田节能节水关键技术研究"(编号:2011E-2402)资助
关键词
柔性复合油管
注水管柱
抗腐蚀
油管强度
试验
flexible composite pipe
water injection string
corrosion resistance
pipe strength
experiment