摘要
安塞油田属于典型低渗透油藏,油井大多采用压裂方式投产,随着注水开发时间的延长,使得人工裂缝和天然裂缝沟通能力进一步增强,导致油井含水率逐渐上升,甚至水淹。为此,安塞油田开展了高含水油井堵水压裂工艺试验与优化,通过屏蔽原有水流通道后再进行压裂改造,达到控水增油目的,充分挖掘高含水油井剩余油,提高油井采收率,为同类油藏高含水井治理提供了一定的借鉴与指导。
Ansai oilfield is a typical low-permeability reservoir, where most wells by fracturing mode of production.With the prolongation of water injection development,the artificial frac- ture and natural fracture communication capacity further enhanced,which cause water cut of well rising,even flooded.So,the water plugging and fracturing technology has been tested and optimized,to fully tap the remaining oil in high water cut wells,and increase its ultimate re- covery,by masking the original flow channel after fracturing, to provide reference and guid- ance for the similar reservoir in high water ~l^t rill w,~ll
出处
《石油化工应用》
CAS
2013年第9期39-42,共4页
Petrochemical Industry Application
基金
长庆油田分公司科研项目"老油田油井控水增油技术研究与应用"
关键词
高含水井
堵水压裂
试验与优化
high water-cut wells
water plugging and fracturing technology
test and optimization of process