摘要
分析了聚乙烯装置在开车期间存在的主要问题,结合历年开车数据和生产经验,提出了具体的控制措施。回收利用蒸汽冷凝水至流化床反应器(R-401)的冷却系统,以提高循环冷却水温度;优化置换方法,细化R-401系统复位前的确认工作;优化R-401内床层料位、床层分配率和循环气体组分的浓度,以及超临界环管反应器内氢气浓度等的方法。减少了置换次数6次,缩短开车期间的排放时间9.0 h,缩短开车时间8.0 h,减少了氮气用量35 700 m3,减少开车期间乙烯、1-丁烯、丙烷和氮气排放量各1.5,0.1,14.5,19.9 t,增加产量510 t,达到预期效果。
The author analyzed the main problems during the start-up on the polyethylene plant. According to the historical start-up data and production experience, some controlling measures were taken, such as recycling condensate water to the cooling system of the fluidized-bed reactor R-401 in order to increase the cooling water temperature, optimizing method of substitution, defining confirmation items before R-401 system resetting, and optimizing controlling methods for fluidized-bed level, bed split and circulation gas ratio in R-401 and hydrogen concentra tion in the supercritical loop reactor. By the above effective measures, substitution was decreased by six times, discharge time was shortened by nine hours, start-up time was shortened by eight hours, nitrogen usage was reduced by 35 700 m3, discharge amounts of ethylene,1-butene, propane and nitrogen were reduced by 1.5, 0.1, 14.5 19.9 t, respectively. Consequently, the yield was increased by 510 t, and the desired effect was achieved.
出处
《合成树脂及塑料》
CAS
北大核心
2014年第1期47-50,55,共5页
China Synthetic Resin and Plastics
关键词
聚乙烯
流化床反应器
优化
置换
循环气冷却器
polyethylene
fluidized-bed reactor
optimization
substitution
circulation gas cooler