摘要
为了更进一步研究陷落柱的突水机理,完善陷落柱突水的试验基础,通过自制的一套变质量破碎岩体渗流试验系统,对变质量破碎岩体非Darcy流渗透特性进行试验,并对破碎泥岩在渗流过程中质量流失量、孔隙度、渗透率、非Darcy流β因子及加速度系数的时变规律进行了研究。研究表明:泥岩试样在渗流过程中渗流形式发生了巨大的变化。在渗流开始时,流失质量迅速增加,引起试样内部孔隙结构变化,孔隙度增加,试样的渗透性能增强,试样压得越密实,质量流失量越多,孔隙度变化越快,渗透性能越强。质量流失量与渗透性是相互影响的,由于试验中质量流失具有时变性特征,渗透性能也具有时变性。最后,陷落柱突水过程可以描述为,在其底部承压水压力作用下,大量细小颗粒随水流一起迁移流失,引起柱体内孔隙度变大,渗透性加强,导致渗流剧变,引发突水。
In order to study water - inrush mechanism of collapse column and complete testing basis for water inrush of collapse column, a self - designed seepage testing system for variable mass of broken rock was used to testing the nonlinear seepage characters of variable mass of broken mudstone. The time - changed laws of losing weight, porosity, permeability, non - Darcy flow/3 factor of mudstone dur- ing the seepage process were researched. It shows that the seepage form of mudstone sample changed enormously during the seepage process ; at the beginning of seepage, the losing weight increased rapidly, which caused the interior pore structure changing, porosity in- creasing and the permeability quality enhancing; the denser of the broken mudstone compressed, the larger of the losing weight was ; the faster porosity of sample changed, the better of the permeability quality was ; the losing weight and permeability were interacted with each other; the losing weight in the test had time -changed character, as well as permeability parameters. Finally, the process of water in- rush of collapse column could be explained as follow, a large number of fine particles were lost with flow under confined ground water, which caused porosity increasing, permeability quality enhancing, and resulting in seepage great changing and water inrush.
出处
《煤矿安全》
CAS
北大核心
2014年第2期15-17,21,共4页
Safety in Coal Mines
基金
国家重点基础研究发展计划(973计划)资助项目(2013CB227900)
国家自然科学基金委员会
神华集团有限责任公司联合资助项目(U1261201)
国家自然科学基金资助项目(50974107
51304072)
关键词
变质量
破碎岩体
渗透特性
非线性渗流
时变
突水
陷落柱
variable mass
broken rock
permeability parameter
nonlinear seepage
time - changed
water - inrush mechanism
col- lapse column