摘要
采用电加热循环流化床锅炉模拟实际烟气,在炉膛出口喷入氨水或同时添加H2、CH4进行脱硝,实验结果表明:最佳停留时间、氨氮物质的量之比分别为0.6,s和1.5,氨水最佳反应温度为920,℃,添加H2最佳温度降低至750,℃,添加CH4最佳温度降低至840,℃.同时为深入认识其化学反应规律,采用基元反应动力学模型对氨水与NOx反应进行了模拟计算,模拟结果表明,该基元反应模型较好地解释了反应机理.
In this work, simulated circulating fluidized bed (CFB) flue gas was fed into an electricity-heated tubular flow reactor, and ammonia was injected into the flue gas as a reducing agent. Besides, H2 or CH4 was added to the flue gas for denitrification and its effects on selective non-catalytic reduction (SNCR) process were explored. Experimental results show that the maximum reduction was achieved at the optimal temperature of 920℃, with the residence time of 0.6 s and a normalized NH3/NOx stoichiometric ratio of 1.5. The optimal temperature is reduced to 750 ℃ with H2 as an additive and to 840 ℃ with CH4 as an additive. Besides, in order to explore the reaction characteristics of SNCR and SNCR with H2 or CH4 addition, the chemical reaction mechanism was analyzed by one business software. By comparison between the experimental data and the calculation results, the selected mechanism was found to be agreeable in forecasting the process.
出处
《燃烧科学与技术》
EI
CAS
CSCD
北大核心
2014年第2期101-105,共5页
Journal of Combustion Science and Technology
基金
国家科技支撑计划子课题资助项目(2012BAA02B01-05)
关键词
循环流化床
选择性非催化还原
脱硝
circulating fluidized bed (CFB)
selective non-catalytic reduction, SNCR
denitrification