摘要
在宝兴水电站引水隧洞底板施工过程中,通过现场浮碴混凝土底板抗外水抬动试验,并参考类似工程经验,对原素混凝土底板施工方案进行了优化,在部分Ⅱ-Ⅲ类围岩洞段采用浮碴混凝土底板,简化了底板清理的施工工序,降低了底板混凝土厚度,增加了混凝土底板及边墙排水孔,对控制投资、加快施工进度起到了积极作用。
For the diversion tunnel of Baoxing Hydropower Project,field floating ballast concrete floor slab lifting test against external water pressure was conducted during construction. With reference to the testing results and the experience of similar projects,the original plain concrete floor slab construction scheme was optimized and floating ballast concrete floor slab scheme was adopted for the tunnel sections with II^III category surrounding rock ,which had played an active role in cost control and accelerating construction progress due to simplified floor slab cleaning procedures,reduced concrete slab thickness,increased drainage holes on base slab and walls.
出处
《广西水利水电》
2014年第4期57-58,70,共3页
Guangxi Water Resources & Hydropower Engineering
关键词
引水隧洞
浮碴
底板外水压力
抬动试验
宝兴水电站
Diversion tunnel
floating ballast
external water pressure on floor slab
lift test
Baoxing Hydropow-er Project