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优化控制在135MW循环流化床锅炉的应用

The Application and Practice of Optimizing Control to Circulating Fluidized Bed Boilers
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摘要 目前国内的循环流化床自动化投入率普遍较低,对控制策略提出了更高的要求,以增强电厂的整体效益和竞争力。但由于循环流化床机组特有的燃烧特性,常规PID控制策略很难实现循环流化床锅炉燃烧自动控制,导致循环流化床锅炉机组的自动投入率低。优化控制系统在循环流化床锅炉燃烧控制的应用,为此提供了一种良好的解决途径。 Now, the input rate of automated circulating fluidized bed is prevailingly low. Thus, in order to promote the whole profit and competitive strength, the higher demand for DCS system is proposed. But, because of the peculiar combustion characteristics of circulating fluidized bed unit, it is hard to realize automated control of CFB boiler combustion by means of regular PID control strategy, which can lead to low rate of automated input of CFB boiler unit and the fail of boiler - turbine cooperative control. In these cases, the application of optimizing control to CFB unit combustion control offers an effective resolution.
出处 《应用能源技术》 2014年第9期28-33,共6页 Applied Energy Technology
关键词 优化控制系统 无辨识自适应控制 循环流化床锅炉 分散控制系统 Optimizing control system XD - APC Identification - free adaptive control CFB boiler DCS
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