摘要
目的提高铝合金铸锻联合成形工艺毛坯冲制良品率。方法采用优化模具设计、设备配置,增加模具保温、坯料预润滑和坯料预处理工序等综合治理方法,开展生产实验研究。结果铝合金铸锻联合成形工艺毛坯冲制良品率由原来的不足85.63%,提高到了97%的稳定水平。结论7A04铸铝坯料的冲制成形条件,比7A04挤压棒材的冲制成形条件要求高,用7A04铝合金铸造坯料代替7A04铝合金棒材冲制工件时,必须对毛坯冲制成形工艺进行细致的完善。
Objective To increase the roughcast conformity rate of the aluminum alloy cast forge composite forming technology. Methods Comprehensive measures including optimization of mould design,equipment configuration,increasing temperature holding feature of the mould,beforehand lubricating and pretreatment of the blank material were adopted,and production experimental study was conducted. Results Aluminum alloy cast forge composite forming technology increased the roughcast conformity rate from below 85. 63% to stably 97%. Conclusion The cast forming condition of 7A04 cast aluminium material had higher requirements than those of 7A04 extrusion bar material. When 7A04 aluminium alloy casting material was used to replace the 7A04 aluminium alloy bar material for workpiece casting,the casting and forming technology for the semifinished material should be refined.
出处
《精密成形工程》
2014年第4期79-84,共6页
Journal of Netshape Forming Engineering
关键词
铝合金
冲制毛坯
质量控制
aluminum alloy
roughcast
quality control