摘要
针对桩129-1HF井摩阻扭矩大、携岩困难、井壁失稳突出等问题,在分析大位移井钻井中钻井液技术难点的基础上,通过评价悬浮剂CDXW的悬浮能力和携岩能力、高效润滑剂BH-1在常温和高温高压条件下的润滑效果,以及优化粒度级配、优选页岩抑制剂,形成了铝胺基聚磺钻井液,并对其性能进行了评价。结果表明,铝胺基聚磺钻井液的API滤失量小于3mL,高温高压滤失量小于10mL,动塑比在0.5以上,黏附系数小于0.05,说明该钻井液抗温性能好,携岩能力强,润滑性能可以满足大位移井的润滑要求。桩129-1HF井使用铝胺基聚磺钻井液钻进的井段,起下钻正常,没有发生井下故障,三开油层段平均井径扩大率仅为3.85%,钻井周期比设计周期缩短了22.09d。这表明铝胺基聚磺钻井液具有良好的携岩能力、润滑性和抑制性,能有效解决大位移井井眼清洁效果差、摩阻和扭矩大等问题。
Based on the analysis of technical difficulties of extreme friction, cuttings transport and bore hole stabilization in Zhuang 129-1HF extended reach well, aluminum-amine based polysulfonate drilling fluid was developed. It had optimized grade distribution and shale inhibitor through the experimental evalu- ation of the suspension and cuttings carrying ability for suspending agent CDXW. The fluid was also ana- lyzed to determine its lubrication of lubricator BH 1 under both ambient temperature and HPHT condi- tions. API filtrate loss of the developed drilling fluid was less than 3 mL, HTHP filtrate loss of the developed drilling fluid was less than 10 mL,the yield point and plastic viscosity ratio is over 0. 5 and the adhe- sion coefficient is less than 0.05. The results indicated that this drilling fluid can be characterized as having good resistance to high temperature, is excellent for cuttings carrying and lubricating. Field drilling applica- tion shows that borehole enlargement ratio was within 3.85%, drilling period shortened by 22.09 days, which demonstrates that the aluminum-amine based polysulfonate drilling fluid is excellent in rock carry- ing, lubricity and inhibition, and can effectively solve the problems of poor hole cleaning and great friction.
出处
《石油钻探技术》
CAS
CSCD
北大核心
2014年第6期34-39,共6页
Petroleum Drilling Techniques
基金
国家高技术研究发展计划("863"计划)项目"海上大位移井钻完井关键技术开发与集成"(编号:2012AA091501)
中石化胜利石油工程有限公司重点课题"大位移井钻井液关键技术研究"(编号:GKZ1202)部分研究内容
关键词
大位移井
钻井液
钻井液性能
钻井液添加剂
桩129-1HF井
extended reach well
drilling fluid
drilling fluid property
drilling fluid additives
Well Zhuang 129-1HF