摘要
某超临界600 MW机组旋流对冲燃烧锅炉低氮改造后,由于运行调整不理想,致使锅炉尾部C O浓度偏高且N Ox 排放未达到预期目标.分析认为,其主要原因是锅炉沿炉膛宽度及深度方向氧量分布不均所致.对此,根据燃烧器改造后的结构特点,对燃烧器参数进行优化调整,在保证NOx 排放的前提下将锅炉满负荷时尾部 CO 浓度由2000μL/L 左右降至100μL/L以下,飞灰可燃物含碳量降至0.5%以下,锅炉效率提高0.8百分点,NOx 排放浓度由改造前的400~450 mg/m3降至250 mg/m3左右.
After low-NOx burner transformation of a supercritical 600 MW swirl-opposed firing boiler,the CO concentration in the tail became high and the NOx emission didn't reach the expectations due improper operation adj ustment.The analysis shows that the uneven distribution of oxygen along the width and depth direction of the furnace is the main cause.Thus,according to the structural characteristics of the retrofited burners,the burner parameters were optimized.After that,the CO concentration at rated load reduced from 2 000μL/L to lower than 100μL/L,the carbon content in fly ash reduced to below 0.5%,the boiler effi-ciency increased by 0.8%,and the NOx emission concentration dropped from 400~450 mg/m3 to about 2 5 0 mg/m3 .
出处
《热力发电》
CAS
北大核心
2014年第12期82-88,共7页
Thermal Power Generation
基金
中国华能集团公司科学技术项目(600MW超临界发电机组整体性能优化与工程示范
HNKJ12-H03)
关键词
锅炉
低NOx旋流燃烧器
CO浓度
NOX排放
氧量分布
燃烧调整
锅炉效率
boiler
low NOx swirl burner
CO concentration
NOx emission
oxygen distribution
combustion adj ustment
boiler efficiency