摘要
由于1 000 MW超超临界机组抽汽逆止阀门活动试验只能在现场通过活动手柄进行、并且部分抽汽逆止门位置较高、存在不安全因素及劳动强度大等问题。通过对抽汽逆止阀门控制气路和动作原理的分析,将控制气路进行改造,从而实现在DCS操作系统中进行抽汽逆止阀门活动试验,解决了现场试验环境不利等因素,提高了1 000 MW超超临界机组的自动化水平。
The flexibility test of the steam extraction non-return valve of a 1 000 MW ultra-supercritical can be only conducted on the spot by using the mobile handle and a part of steam extraction non-return valves are located at a relatively high positions,thus there exist some unsafe factors and a strong laboring strength etc. Through an analysis of the control air circuit and working principles of the steam extraction non-return valve,a modification was made to the control air circuit,thus realizing a flexibility test of a steam extraction non-return valve conducted in a DCS operation system,solving the problem that the on-the-spot test environment is adverse and enhancing the automation level of 1 000 MW ultra-supercritical units.
出处
《热能动力工程》
CAS
CSCD
北大核心
2015年第2期306-308,328,共3页
Journal of Engineering for Thermal Energy and Power
关键词
1000
MW超超临界机组
汽轮机
抽汽逆止阀门
活动试验
自动化
优化改造
1 000 MW ultra-supercritical unit,steam turbine,steam extraction non-return valve,flexibility test,automation,optimized modifica