摘要
华电白音华金山发电有限公司#1,#2汽轮机高、低压加热器上、下端差都较设计值明显偏高,最大端差偏离设计值13.94℃。采集了300,400和565 MW 3个工况的参数进行分析,得出端差大的原因为加热器水位以及各段抽汽温度超标并提出了相应的处理措施。
In Huadian Baiyinhua Jinshan Power Company Limited,#1,#2 turbines' high and low pressure heaters' terminal temperature differences are sharply higher than the designed value,with a maximum deviation of 13. 94 ℃. After analyzing parameters collected from 300,400 and 565 MW,causes are concluded that both the heaters' water level and the extraction steam temperature exceeded standard values; and measures are put forward.
出处
《华电技术》
CAS
2015年第4期36-38,77-78,共3页
HUADIAN TECHNOLOGY
关键词
加热器
热工测点
水位
抽汽温度
heater
thermal measurement
water level
extraction steam temperature