期刊文献+

炼油厂重催装置分馏塔顶换热器管束的腐蚀失效分析 被引量:3

Corrosion Failure Analysis of Heat Exchanger Tube Bundle in Oil Refinery Residue Fluid Catalytic Cracking Unit Fractionating Tower Top
下载PDF
导出
摘要 某炼油厂重催装置分馏塔顶换热器管束在使用18个月后发生了腐蚀失效,采用扫描电镜、能谱仪和X射线衍射仪等对失效原因进行了分析。结果表明:换热管外表面发生了严重的点蚀,最大腐蚀坑深度为0.98 mm,达到了管壁厚度的40.3%;换热管外表面的腐蚀产物主要有α-FeO(OH)、Fe2O3、Fe3O4、FeS和FeCl2;换热管外表面所处介质环境中的腐蚀性离子(Cl-和S2-)含量很高,这是导致换热器管束腐蚀失效的主要原因。 Corrosion failure of heat exchanger tube bundle in oil refinery residue fluid catalytic cracking unit fractionation tower top occured after using for 18 months, the causes were analyzed by scanning electron microscopy, energy disperse spectroscopy and X-ray diffraction. The results show that the outer surface of the heat exchange tube exhibited serious pitting, the maximum depth of corrosion pits was 0. 98 ram, accounting for 40. 3% of the tube thickness. The corrosion products on the outer surface of the heat exchange tube were mainly α-FeO(OH), Fe2O3, Fe3O4, FeS and FeCl2. The content of corrosive ions (Cl and S2- ) in the media around heat exchange tube outer surface was very high, this was the main reason leading to corrosion failure for heat exchanger tube bundle.
出处 《机械工程材料》 CAS CSCD 北大核心 2015年第5期102-106,共5页 Materials For Mechanical Engineering
基金 陕西省教育厅专项科研计划项目(2013JK0895) 陕西省重点学科专项资金资助项目
关键词 换热管 局部腐蚀 腐蚀产物 腐蚀失效 渗铝钢 heat exchange tube local corrosion corrosion product corrosion failure aluminized steel
  • 相关文献

参考文献13

二级参考文献71

共引文献95

同被引文献34

引证文献3

二级引证文献11

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部