摘要
预分解窑内形成后结圈,既影响窑的台时产量,又影响熟料的质量。文章主要论述了预分解窑形成后结圈的现象和原因,以及在生产实践中采取的应对措施:(1)控制进厂原材料的质量;(2)控制进厂原煤的质量;(3)稳定生料的质量;(4)改变熟料配料方案,采取高KH(0.91±0.02)和较低SM(2.65±0.1)的配料方案;(5)优化操作参数。结果表明,窑产量平均提高79 t/d,全年多产熟料2.6万t;熟料标准煤耗降低4.19 kg/t,全年节约标准煤6 400 t,二项累计创直接经济效益616万元。
Clinker ring formation in precalciner kiln has effeet on output of kiln and the quality of clinker. This paper mainly discusses the phenomenon and reasons of ring formation in preealciner kiln and takes measures in production practice: (1) Control the quality of raw materials;(2)Control the quality of raw coal ;(3) Stabilize the quality of raw materials;(4) change the ingredients of clinker and take ingredients scheme of high KH (0.91 ±0,02) and low SM (2.65±0.1);(5) optimize operating parameters. The result shows that the kiln production increases an average of 79 t/d, produces 26 000 t more one year; Standard coal consumption of clinker reduces 4.19 kg/t, saving standard coal 6400 t/a.Both methods creates direct economic returns about 6.16 million yuan.
出处
《水泥工程》
CAS
2015年第4期28-30,共3页
Cement Engineering
基金
"重庆市高等教育学会2013-2014年高等教育科学研究课题(项目名称:高职院校与企业合作长效机制的研究
项目编号:CQGJ13C767)"的阶段性研究成果
关键词
预分解窑后结圈
现象
原因分析
技术措施
ring formation after preealciner kiln
analyse of phenomenon and reason
technical measures