摘要
"W"火焰锅炉为了燃烧难燃无烟煤,通常采取高煤粉浓度、高温、高氧量集中送风、高停留时间方式组织燃烧,而高氧量集中送风是造成锅炉NOx排放浓度高达1 200-2 000 mg/m^3的主要原因。某电厂300 MW机组采用"W火焰"燃烧方式,NOx排放浓度约600-1 300 mg/m^3。为了能够节能减排,通过燃烧器、分级配风、卫燃带这三个方面进行了低氮燃烧改造。改造后NOx排放浓度达到了预期改造效果,将脱硝入口NOx排放浓度降低到800 mg/m^3以下。针对改造后产生的锅炉严重结渣问题,采用卫燃带改造的方法进行解决。
In order to combust hard anthracite,pulverized coal with high concentration,high temperature,central air supply with high oxygen content,high resident time to organize combustion were utilized in W shaped flame boiler. However,central air supply with high oxygen content is the main reason why boiler's NOx emission concentration reaches 1 200 - 2 000 mg / m^3. A power plant with 300 MW unit used "W shaped flame"combustion mode and NOx emission content was about 600 - 1 300 mg / m^3. In response to national policy of energy saving and emission reduction,low-nitrogen retrofit was conducted through burner,staged air distribution and refractory belt.The results show that NOx emission content reached expected goal and it was lower than 800 mg / m^3 at the entrance of denitration facility after retrofit. And serious problem of slag bonding after retrofit was solved by refractory belt reconstruction.
出处
《电力科学与工程》
2015年第11期54-58,共5页
Electric Power Science and Engineering
关键词
“W”火焰
NOx排放浓度
低氮燃烧改造
结渣
W shaped flame
NOx emission concentration
low-nitrogen retrofit
slag bonding