摘要
介绍了宾金直流输电线路金华换流站极Ⅱ±800 k V直流穿墙套管发生故障后,接地极线路断线故障过程。采用EMTP-ATP软件对故障前后系统电流为5 970 A和5 215 A时接地极导线和避雷线分流情况进行了仿真计算,并与录波图进行了比较。根据计算结果分析了绝缘子掉串及导线断线原因,以及避雷线熔断原因。提出了接地极线路绝缘配置建议。
Alter fault occurred on +800 kV DC wall bushing of pole II in Jinhua converter station, the grounding line also has breakage fault. By using ATP-EMTP, response of grounding electrode conductor and shielding wire is sinmlated with 5 970 A and 5 215 A fauh current. The results are compared with recorded fault waveform. According to calculation results, the breakage reasons of insulator string and shielding wire are analyzed in detail. The recommended grounding line insulation configuration is also intrudueed.
出处
《中国电力》
CSCD
北大核心
2017年第4期77-80,86,共5页
Electric Power
关键词
±800
KV
接地极
导线
避雷线
断线故障
+800 kV
earth electrode
power conductor
shielding wire
transmission line breakage fault