摘要
华北某城市污水厂实际进水NH_3-N值和SS值均高于设计值。运营以来,由于部分曝气设施老化,好氧池实际泥龄短,生存的硝化菌数量不能实现氨氮稳定达标的要求而导致实际出水水质不能稳定达标。通过提高好氧段实际水力停留时间、校核剩余污泥排放能力、改进生化池缺氧段等技术措施,提高好氧池硝化能力,使NH_3-N及主要水质指标达到城镇污水处理厂污染物排放标准(GB18918-2002)一级A标准。
he actual influent values of NH3-N and SS of a sewage plant in North China were higher than design values. Sinceoperation, because some aeration facilities age and the practical sludge age of aerobic pool was short, the number of survived nitrifying bacteria could not meet the requirement of ammonia nitrogen stabilization standards, so that the practical effluent quality could not met the standard steadily. By improving the actual residence timeofaerobicperiod, checking the residual sludge discharge capacity, improvingtechnicalmeasuresoffhebiochemicalpoolanoxicperiod, enhancing nitrification ability of aerobic pool, to make NH3-N and the main water quality indexes meet the in'st level A discharge standard of pollutants for municipal wastewater treatment plant (GB 18918-2002).
作者
柳利魁
张萌
刘俊良
张淑萍
毕荫来
LIU Likui ZHANG Meng LIU Junliang ZHANG Shuping BI Yinlai(Institute of Urban and Rural Construction, 071000 Agricultural University of Hebei, 071051, Baoding, China)
出处
《水处理技术》
CAS
CSCD
北大核心
2017年第5期123-125,共3页
Technology of Water Treatment
关键词
城市污水
A2/O工艺
高氨氮
污泥负荷
municipal sewage
A2/O process
high ammonia nitrogen
sludge loading