摘要
为改善国内某厂在浇注亚包晶钢时出现的严重表面纵裂问题,对结晶器原水口出口结构进行了改进,并采用实验室1:1水模型研究了水口改进对结晶器流场的影响。结果表明,使用改进水口后,结晶器内液面波动与表面流速均有所降低。通过对该厂水口改进后结晶器内流场的现场测量,发现液面波动处于±3mm范围内的比例由80%增至90%以上,结晶器内外弧面平均热流量分别减少0.21,0.20MW/m^2,促进了结晶器的缓冷,改善了高质量亚包晶钢板坯的生产条件。
In order to improve bad surface longitudinal cracks during casting hypo-periteetic steel in a certain plant, the old mold SEN outlet structure was optimized, and advanced influence to the new mold flow fields was studied through 1:1 scale water model experiments. Results showed that both mold level fluctuation and surface velocity were reduced with the application of new SEN. From the on- site measurement data of new SEN flow fields, the proportion of mold level fluctuations within the range of ±3 mm was increased from 80% to more than 90%. Meanwhile, the average heat fluxes of inner and outer arc sides of mold were reduced 0. 21 MW/m^2 and 0. 20 MW/m^2 respectively, which enhanced mold slow cooling and made high quality hypo-peritectic slab production better.
作者
尹娜
景财良
李海波
刘国梁
YIN Na JING Cailiang LI Haibo LIU Guoliang(Shougang Research Institute of Technology Beijing Key Laboratory of Green Recyclable Process for Iron & Steel Production Technology Shougang Jingtang United Iron & Steel Co., Ltd.)
出处
《首钢科技》
2017年第2期6-11,共6页
Shougang Science and Technology