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某型涡轴发动机喘振攻关与验证 被引量:4

Research on a Certain Type of Turbine Shaft Engine Surge
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摘要 针对某型涡轴发动机夏季试车时常发生加速喘振故障的问题,使用故障树初步分析引起喘振的主要原因,并通过径向扩压器叶片进行流场仿真、串装、多台发动机对比计量、试车试验等,对喘振原因进行深入分析。研究表明径向扩压器进口叶根倒角变大对发动机加速性能有一定程度的改善作用,大气条件对发动机加速性有一定影响,径扩面积越大、叶根圆角与进气边转接越顺滑,越有利于加速性能。 For the problem of turbine shaft engine surge during the acceleration phase in summer, fault tree analysis was used to analyze the main reasons preliminarily. The methods of flow field simulation of radial diffuser blade, replace main parts, comparative analysis of multiple engines and commissioning test were used to analyze the reasons deeply. The result showed that blade root chamfering became larger conduce to acceleration, atmospheric environment reacted on the problem also. The area of radial diffuser, the smoothness of the connect area of blade root chamfering and inlet had great influence on the surge during the acceleration phase.
作者 詹洪飞 黄帅
出处 《海军航空工程学院学报》 2017年第3期295-301,共7页 Journal of Naval Aeronautical and Astronautical University
关键词 涡轴发动机 喘振 流场仿真 试车试验 turbine shaft engine surge flow field simulation commissioning test
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