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低硫钢种的低硅精炼技术 被引量:5

Low silicon control for steel grades with low sulphur mass percent
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摘要 讨论了冶炼低硅低硫钢种(w([S])≤0.003 0%和w([Si])≤0.05%)的难点,着重从热力学角度分析了在脱硫的同时防止增硅的方法,阐述了防止增硅的具体应对措施。利用Factsage软件计算熔渣组成的活度和熔化特性,利用最大平衡铝质量分数的概念指出最佳的精炼熔渣组分控制为w((MgO))=5%-8%、w((CaO+MgO))=62%-66%、w((SiO2))=4%-6%、w((Al2O3))=29%-33%。若钢-渣间反应达到平衡,硅质量分数极为容易超标,因此控制钢-渣之间反应不平衡是控制增硅的关键,钢-渣间增硅反应不平衡度应控制在-6.0--4.0。措施实施后,LF炉精炼结束硅质量分数均值由0.034 5%降低至0.022 2%,统计不合格率由10.3%降至0,过程能力指数Cpk值为1.35,达到受控状态,预测长期不合格率仅为0.2%。极大提升了低硫低硅产品生产的稳定性,取得了良好的效益。 The way to control the silicon content when w([S])≤0.003 0% and w([Si])≤0.05% was introduced. Factsage was used to calculate the activities and other melting characteristics of melted slags,following with maxium aluminium content in metal,which showed the optimized slag composition are,w((MgO))= 5%-8%,w((CaO+MgO))= 62%-66%,w((SiO2))= 4%-6%,w((Al2O3))= 29%-33%. It was revealed that the silicon content will exceed the upper limit when slag-metal reactions go balanced. So the imbalance degree of slag-metal reactions plays the biggest role in controlling silicon pickup,which should range between-6.0 and-4.0. Some actions were signed and applied,consequence in average silicon content decreasing from 0.034 5% to 0.022 2%,unqualified rate decreasing from 10.3% to 0,process capability index 1.35,and the predicted unqualified ratio 0.2%. This dramatically improved the stability of the production process of low silicon and sulphur grades.
作者 陈玉鑫 陈峰 温瀚 王朝斌 CHEN Yu-xin;CHEN Feng;WEN Han;WANG Chao-bin(BJ Office,KERNEOS(CHINA)Aluminates Technologies Co.,Ltd.,Beijing 100028,China;Steel Plant,Shougang Jingtang Iron and Steel United Co.,Ltd.,Tangshan 063200,Hebei,China)
出处 《钢铁》 CAS CSCD 北大核心 2018年第7期60-67,共8页 Iron and Steel
关键词 精炼渣 不平衡度 回硅 低硫低硅钢种 脱硫 硫分配比 refining flux imbalance degree silicon pickup low silicon and suphur steel desulphurization sulphur partition ratio
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