摘要
The design and running effect of treatment of wastewater from pharmaceutical intermittent production by iron-carbon(Fe/C)-Fentonhydrolysis acidification-anoxic/aerobic(A/O)process were introduced.The results of continuous operation showed that when the flow rate of the influent wastewater was 300 m^3/d,after the influent high-concentration wastewater(CODCrand NH4+-N concentration were 35 000 and 1 000 mg/L,respectively)and medium-concentration wastewater(CODCrand NH4+-N concentration were 1 500 and 100 mg/L,respectively)were treated by the process,CODCrand NH4+-N concentration in the effluent decreased to 360-410 and 20-25 mg/L,respectively,and the quality of the effluent could meet the Grade III standard of Integrated Wastewater Discharge Standard(GB 8978-1996).The combined process was proved to be an effective method to treat wastewater from pharmaceutical intermittent production,and its operation was stable.
The design and running effect of treatment of wastewater from pharmaceutical intermittent production by iron-carbon(Fe/C)-Fentonhydrolysis acidification-anoxic/aerobic(A/O)process were introduced.The results of continuous operation showed that when the flow rate of the influent wastewater was 300 m^3/d,after the influent high-concentration wastewater(CODCrand NH4+-N concentration were 35 000 and 1 000 mg/L,respectively)and medium-concentration wastewater(CODCrand NH4+-N concentration were 1 500 and 100 mg/L,respectively)were treated by the process,CODCrand NH4+-N concentration in the effluent decreased to 360-410 and 20-25 mg/L,respectively,and the quality of the effluent could meet the Grade III standard of Integrated Wastewater Discharge Standard(GB 8978-1996).The combined process was proved to be an effective method to treat wastewater from pharmaceutical intermittent production,and its operation was stable.