摘要
针对中石化首座凝析气田循环高压注气工程—大涝坝注气压缩机组运行以来频繁出现的无油流报警停机,从机组的结构及工作原理入手,对润滑系统和控制系统等方面进行分析,查找产生问题的原因及症结,提出了相应的处理方法及对应的改进措施,使注气压缩机组的故障率降低,保障了机组的安全平稳运行。
Based on the structure and working principle of the unit, the lubrication system and the control systemare analyzed to find out the cause and the crux of the problem, and the corresponding treatment methods and cor-responding improvement measures are put forward. The failure rate of the gas injection compressor unit is re-duced, thus ensuring the safe and stable operation of the unit.
出处
《新疆石油天然气》
CAS
2018年第2期92-96,共5页
Xinjiang Oil & Gas
关键词
高压注气压缩机
无油流报警
注油分配块
分析与处理
天然气放空
Gas injection compressor
Oil free flow alarm
Oil injection distribution block
Analysis and treatment
Natural gas vent